Altitude-Wind-Tunnel Investigation of Westinghouse 19B-2 19B-8, and 19XB-1 Jet-Propulsion Engines, Part 1, Operational Characteristics

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From Summary: "An investigation was conducted in the NACA Cleveland altitude wind tunnel to determine the operational characteristics of the Westinghouse 19B-2, 19B-8, and 19XB-l jet-propulsion engines. The 19B engine is one of the earliest experimental Westinghouse axial flow engines. The 19XB-1 engine is an experimental prototype of the Westinghouse 15 series, having a rated thrust of 1400 pounds. Improvements in performance and operational characteristics have resulted in the 19XB-2B engine with a rated thrust of 1600 pounds. The operational characteristics were determined over a range of simulated altitudes from 5000 to 30,000 feet for the 19B engines and from … continued below

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21 p. : ill.

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Fleming, William A. November 22, 1948.

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This report is part of the collection entitled: National Advisory Committee for Aeronautics Collection and was provided by the UNT Libraries Government Documents Department to the UNT Digital Library, a digital repository hosted by the UNT Libraries. It has been viewed 317 times. More information about this report can be viewed below.

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  • Main Title: Altitude-Wind-Tunnel Investigation of Westinghouse 19B-2 19B-8, and 19XB-1 Jet-Propulsion Engines, Part 1, Operational Characteristics
  • Series Title: NACA Research Memorandums

Description

From Summary: "An investigation was conducted in the NACA Cleveland altitude wind tunnel to determine the operational characteristics of the Westinghouse 19B-2, 19B-8, and 19XB-l jet-propulsion engines. The 19B engine is one of the earliest experimental Westinghouse axial flow engines. The 19XB-1 engine is an experimental prototype of the Westinghouse 15 series, having a rated thrust of 1400 pounds. Improvements in performance and operational characteristics have resulted in the 19XB-2B engine with a rated thrust of 1600 pounds. The operational characteristics were determined over a range of simulated altitudes from 5000 to 30,000 feet for the 19B engines and from 5000 to 35000 feet for the 19XB-l engine at airspeed from 20 to 380 miles per hour."

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21 p. : ill.

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  • URL: http://hdl.handle.net/2060/20050030046 External Link
  • Report No.: NACA-RM-E8J28-Pt-1
  • Center for AeroSpace Information Number: 20050030046
  • Archival Resource Key: ark:/67531/metadc64773

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National Advisory Committee for Aeronautics Collection

The National Advisory Committee for Aeronautics (NACA) was a U.S. federal agency founded on March 3, 1915 to undertake, promote, and institutionalize aeronautical research. On October 1, 1958 the agency was dissolved, and its assets and personnel transferred to the newly created National Aeronautics and Space Administration (NASA).

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  • November 22, 1948

Added to The UNT Digital Library

  • Nov. 17, 2011, 5:13 p.m.

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  • April 9, 2018, 9:21 a.m.

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Fleming, William A. Altitude-Wind-Tunnel Investigation of Westinghouse 19B-2 19B-8, and 19XB-1 Jet-Propulsion Engines, Part 1, Operational Characteristics, report, November 22, 1948; (https://digital.library.unt.edu/ark:/67531/metadc64773/: accessed July 18, 2024), University of North Texas Libraries, UNT Digital Library, https://digital.library.unt.edu; crediting UNT Libraries Government Documents Department.

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