Last year (1948) during the flood period the flow at Grand Coulee fluctuated widely. 2 PM, June 8, 543000 c.f.s.; 4 AM, June 9, 568000 c.f s.; 2 PM, June 9, 543000 c.f.s.; 2 AM, June 10, 573000 c.f.s. A total instantaneous fluctuations of 37,500 c.f.s. was reported. Now there is installed a new control. This control can keep downstream variation within 500 c.f.s. By lowering the lake level prior to the crest period, the drum gates could be used as flood control (1948 high water basis) the drum gate control plus the water turbine discharge (if the lake level had been reduced) could have dropped the crest at Richland three feet. a. Drop in crest at Richland one foot: Electrical loss nominal, b. Drop in crest at Richland two feet: Electrical loss 1 megawatt/foot for six generators. Loss Max possible 13,310 KW each generator, 79,860 KW total (7 days). Capacity 1,170,000 KW Max Loss 6.8% for 7 days to 10 days. c. Drop in crest at Richland three feet: Electrical loss 1 megawatt/foot for 6 generators Max possible 30,100 KW each generator 180,600 KW total 8 days. Capacity 1,170,000 KW Maximum loss 15.4% for 8 to 12 days. Actual loss, we believe is much less: For an eleven foot drop actual capacity dropped from 1,170,000 KW to 1,137,000 KW during the present winter. Contacts were re-established with Grand Coulee Control Engineers with whom we had dealt in the 1948 flood. We indicated to Grand Coulee Management, Mr. Bates, Mr. Newberry, etc., that careless control and lack of cooperation between Coulee and Hanford could be harmful and at times disastrous.