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Performance of a 13-Stage Development Compressor for the J40-WE-24 Engine at Equivalent Speeds from 30 to 112 Percent of Design

Description: The performance of a 13-stage development compressor for the J40-WE-24 engine has been determined at equivalent speeds from 30 to 112 percent of design. The design total-pressure ratio of 6.0 and the design weight flow of 164 pounds per second were not attained, An analysis was conducted to determine the reasons for the poor performance at the design and over-design speed. The analysis indicated that most of the difficulty could be attributed to the fact that the first stage was overcompromised… more
Date: April 9, 1953
Creator: Hatch, James E.; Lucas, James G. & Finger, Harold B.
Partner: UNT Libraries Government Documents Department
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