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Addendum to material selection guidelines for geothermal energy-utilization systems. Part I. Extension of the field experience data base. Part II. Proceedings of the geothermal engineering and materials (GEM) program conference (San Diego, CA, 6-8 October 1982)

Description: The extension of the field experience data base includes the following: key corrosive species, updated field experiences, corrosion of secondary loop components or geothermal binary power plants, and suitability of conventional water-source heat pump evaporator materials for geothermal heat pump service. Twenty-four conference papers are included. Three were abstracted previously for EDB. Separate abstracts were prepared for twenty-one. (MHR)
Date: May 1, 1983
Creator: Smith, C. S. & Ellis, P. F., II
Partner: UNT Libraries Government Documents Department
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High SO{sub 2} removal efficiency testing. Technical progress report, January--March 1996

Description: This project involves testing at six full-scale utility flue gas desulfurization (FGD) systems, to evaluate low capital cost upgrades that may allow these systems to achieve up to 98% SO{sub 2} removal efficiency. The upgrades being evaluated primarily involve using performance additives in the FGD systems. The base project involved testing at the Tampa Electric Company Big Bend station. All five potential options to the base program have been exercised by DOE, involving testing at Hooiser Energy`s Merom Station (Option I), Southwestern Electric Power Company`s Pirkey Station (Option II), PSI Energy`s Gibson Station (Option III), Duquesne Light`s Elrama Station (Option IV), and New York State Electric and Gas Corporation`s Kintigh Station (Option V). The originally planned testing has been completed for all six sites.
Date: April 19, 1996
Creator: Blythe, G.
Partner: UNT Libraries Government Documents Department
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High SO{sub 2} removal efficiency testing: Evaluation of high efficiency test results at Hoosier Energy`s Merom Station

Description: Tests were conducted at Hoosier Energy`s Merom Station 535-MW Units 1 and 2 wet limestone flue gas desulfurization (FGD) systems to evaluate options for achieving high SO{sub 2} removal efficiency. The options tested included use of dibasic acid (DBA) and sodium formate additives as well as operation at higher reagent ratios (higher pH set points). In addition to the tested options, the effectiveness of other potential options was simulated using the Electric Power Research Institute`s FGD Process Integration and Simulation Model (FGDPRISM) after it was calibrated to the system. An economic analysis was done to determine the cost effectiveness of each option. A summary of results is given on the following: SO{sub 2} removal performance; additive consumption; and SO{sub 2} removal upgrade economics.
Date: April 22, 1996
Partner: UNT Libraries Government Documents Department
open access

Summary report: Trace substance emissions from a coal-fired gasification plant

Description: The U.S. Department of Energy (DOE), the Electric Power Research Institute (EPRI), and Louisiana Gasification Technology Inc. (LGTI) sponsored field sampling and analyses to characterize emissions of trace substances from LGTI`s integrated gasification combined cycle (IGCC) power plant at Plaquemine, Louisiana. The results indicate that emissions from the LGTI facility were quite low, often in the ppb levels, and comparable to a well-controlled pulverized coal-fired power plant.
Date: October 16, 1996
Creator: Williams, A.; Wetherold, B. & Maxwell, D.
Partner: UNT Libraries Government Documents Department
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High SO{sub 2} removal efficiency testing. Technical progress report, October--December 1995

Description: This project involves testing at six full-scale utility flue gas desulfurization (FGD) systems, to evaluate low capital cost upgrades that may allow these systems to achieve up to 98% SO{sub 2} removal efficiency. The upgrades being evaluated mostly involve using performance additives in the FGD systems. The ``base`` project involved testing at the Tampa Electric Company Big Bend station. All five potential options to the base program have been exercised by DOE, involving testing at Hoosier Energy`s Merom Station (Option I), Southwestern Electric Power Company`s Pirkey Station (Option II), PSI Energy`s Gibson Station (Option III), Duquesne Light`s Elrama Station (Option IV), and New York State Electric and Gas Corporation`s Kintigh Station (Option V). The originally planned testing has been completed for all six sites. Following the introduction, this report is divided into four sections. Section 2, Project Summary, provides a brief overview of the status of technical efforts on this project. Section 3, Results, summarizes the outcome from technical efforts during the quarter, or results from prior quarter that have not been previously reported. In Section 4, Plans for the Next Reporting Period, an overview is provided of the technical efforts anticipated for the first quarter of calendar year 1996. Section 5 contains a brief acknowledgment.
Date: October 18, 1995
Creator: Blythe, G.
Partner: UNT Libraries Government Documents Department
open access

High SO{sub 2} removal efficiency testing: Results of DBA and sodium formate additive tests at Southwestern Electric Power company`s Pirkey Station

Description: Tests were conducted at Southwestern Electric Power Company`s (SWEPCo) Henry W. Pirkey Station wet limestone flue gas desulfurization (FGD) system to evaluate options for achieving high sulfur dioxide removal efficiency. The Pirkey FGD system includes four absorber modules, each with dual slurry recirculation loops and with a perforated plate tray in the upper loop. The options tested involved the use of dibasic acid (DBA) or sodium formate as a performance additive. The effectiveness of other potential options was simulated with the Electric Power Research Institute`s (EPRI) FGD PRocess Integration and Simulation Model (FGDPRISM) after it was calibrated to the system. An economic analysis was done to determine the cost effectiveness of the high-efficiency options. Results are-summarized below.
Date: May 30, 1996
Partner: UNT Libraries Government Documents Department
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High SO{sub 2} removal efficiency testing. Topical report - results of sodium formate additive tests at New York State Electric & Gas Corporation`s Kintigh Station

Description: Tests were conducted at New York State Gas & Electric`s (NYSEG`s) Kintigh Station to evaluate options for achieving high sulfur dioxide (SO{sub 2}) removal efficiency in the wet limestone flue gas desulfurization (FGD) system. This test program was one of six conducted by the U.S. Department of Energy to evaluate low-capital-cost upgrades to existing FGD systems as a means for utilities to comply with the requirements of the 1990 Clean Air Act Amendments. The upgrade option tested at Kintigh was sodium formate additive. Results from the tests were used to calibrate the Electric Power Research Institute`s (EPRI) FGD PRocess Integration and Simulation Model (FGDPRISM) to the Kintigh scrubber configuration. FGDPRISM was then used to predict system performance for evaluating conditions other than those tested. An economic evaluation was then done to determine the cost effectiveness of various high-efficiency upgrade options. These costs can be compared with the estimated market value of SO{sub 2} allowance or the expected costs of allowances generated by other means, such as fuel switching or new scrubbers, to arrive at the most cost-effective strategy for Clean Air Act compliance.
Date: February 14, 1997
Creator: Murphy, J.
Partner: UNT Libraries Government Documents Department
open access

High SO{sub 2} removal efficiency testing. Quarterly report, July - September 1996

Description: This document provides a discussion of the technical progress on DOE/PETC project number DE-AC22-92PC91338, ``High Efficiency SO{sub 2} Removal Testing,`` for the time period 1 July through 30 September 1996. The project involves testing at six full-scale utility flue gas desulfurization (FGD) systems, to evaluate low capital cost upgrades that may allow these systems to achieve up to 98% SO{sub 2} removal efficiency. The upgrades being evaluated mostly involve using performance additives in the FGD systems. The ``base`` project involved testing at the Tampa Electric Company`s Big Bend Station. All five potential options to the base program have been exercised by DOE, involving testing at Hoosier Energy`s Merom Station (Option I), Southwestern Electric Power Company`s Pirkey Station (Option II), PSI Energy`s Gibson Station (Option III), Duquesne Light`s Elrama Station (Option IV), and New York State Electric and Gas Corporation`s Kintigh Station (Option V). The originally planned testing has been completed for all six sites. The remainder of this document provides a brief overview of the status of technical efforts on this project, including those efforts anticipated for the first quarter of calendar year 1996, summarizes results from prior quarters, and contains a brief acknowledgment. 13 refs.
Date: July 1, 1996
Creator: Blythe, G.
Partner: UNT Libraries Government Documents Department
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High SO{sub 2} removal efficiency testing: PSI Energy`s Gibson Station High SO{sub 2} Removal Efficiency Test Program

Description: A program was conducted at PSI Energy`s Gibson Generating Station to evaluate options for achieving high sulfur dioxide (SO{sub 2}) removal efficiency with the Unit 5 wet limestone flue gas desulfurization (FGD) system. This program was one of six conducted by the U.S. Department of Energy to evaluate low-capital-cost upgrades to existing FGD systems as a means for utilities to comply with the requirements of the 1990 Clean Air Act Amendments (CAAA). The Gibson FGD system employs four absorber modules of the Kellogg/Weir horizontal gas flow design and uses limestone reagent with two additives. Dolomitic lime is added to introduce magnesium to increase liquid-phase alkalinity, and sulfur is added to inhibit sulfite oxidation. The high-efficiency options tested involved using sodium formate or dibasic acid (DBA) as a performance additive, increasing the absorber liquid-to-gas ratio (L/G), and/or increasing the limestone reagent stoichiometry. The unit changed coal sources during the test program. However, the Electric Power Research Institute`s (EPRI) FGD PRocess Integration and Simulation Model (FGDPRISM) was calibrated to the system and used to compare options on a consistent basis. An economic analysis was then done to determine the cost-effectiveness of each high-efficiency option. The results from this program are summarized below.
Date: May 20, 1996
Partner: UNT Libraries Government Documents Department
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High SO{sub 2} removal efficiency testing. Technical progress report, [1 July--30 September 1993]

Description: This document provides a discussion of the technical progress on DOE/PETC project number DE-AC22-92PC91338, {open_quotes}High Efficiency SO{sub 2} Removal Testing{close_quotes}, for the time period 1 July through 30 September, 1993. The project involves testing at six full-scale utility flue gas desulfurization (FGD) systems, to evaluate low capital cost upgrades that may allow these systems to achieve up to 98% SO{sub 2} removal efficiency. The upgrades to be evaluated primarily involve the addition of organic acid buffers to the FGD systems. The {open_quotes}base{close_quotes} project involved testing at the Tampa Electric Company Big Bend station. As of September 1993, all five potential options to the base program had been exercised by DOE, involving testing at the Hoosier Energy Merom Station (Option I), the Southwestern Electric Power Company Pirkey Station (Option II), the PSI Energy Gibson Station (Option III), the Duquesne Light Elrama Station (Option IV), and the New York State Electric and Gas Company Kintigh Station (Option V). As of September 1993, testing has been completed for the base project and for Options 1 and 2, has begun but not been completed for Options III and IV, and has not yet begun for Option V. This document is divided into five sections. After a brief introduction (Section 1), Section 2 (Project Summary) provides a brief overview of the status of technical efforts on this project. Section 3 (Results) summarizes the outcome from these technical efforts during the quarter. Results for each site for which there were significant technical efforts or for which there are updated technical results are discussed in separate subsections. In Section 4 (Plans for the Next Reporting Period) an overview is provided of the technical progress that is anticipated for the fourth quarter of calendar year 1993. Section 5 includes a brief acknowledgement.
Date: October 28, 1993
Creator: Blythe, G.
Partner: UNT Libraries Government Documents Department
open access

Field study of disposed wastes from advanced coal processes. Quarterly technical progress report: April--June 1993

Description: The Department of Energy/Morgantown Energy Technology Center (DOE/METC) has initiated research on the disposal of solid wastes from advanced coal processes. The objective of this research is to develop information to be used by private industry and government agencies for planning waste disposal practices associated with advanced coal processes. To accomplish this objective, DOE has contracted Radian Corporation and the North Dakota Energy & Environmental Research Center (EERC) to design, construct, and monitor a limited number of field disposal tests with advanced coal process wastes. These field tests will be monitored over a three year period with the emphasis on collecting data on the field disposal of these wastes. There has been considerable research on the characteristics and laboratory leaching behavior of coal wastes -- a lesser amount on wastes from advanced coal processes. However, very little information exists on the field disposal behavior of these wastes. Information on field disposal behavior is needed (a) as input to predictive models being developed, (b) as input to the development of rule of thumb design guidelines for the disposal of these wastes, and (c) as evidence of the behavior of these wastes in the natural environment.
Date: December 31, 1993
Partner: UNT Libraries Government Documents Department
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Field study of disposed wastes from advanced coal processes. Quarterly technical progress report, February 1992--April 1992

Description: The Department of Energy/Morgantown Energy Technology Center (DOE/METC) has initiated research on the disposal of solid wastes from advanced coal processes. The objective of this research is to develop information to be used by private industry and government agencies for planning waste disposal practices associated with advanced coal processes. To accomplish this objective, DOE has contracted Radian Corporation and the North Dakota Energy & Environmental Research Center (EERC) to design, construct, and monitor a limited number of field disposal tests with advanced coal process wastes. These field tests will be monitored over a three year period with the emphasis on collecting data on the field disposal of these wastes. There has been considerable research on the characteristics and laboratory leaching behavior of coal wastes -- a lesser amount on wastes from advanced coal processes. However, very little information exists on the field disposal behavior of these wastes. Information on field disposal behavior is needed (a) as input to predictive models being developed, (b) as input to the development of rule of thumb design guidelines for the disposal of these wastes, and (c) as evidence of the behavior of these wastes in the natural environment.
Date: December 1, 1992
Partner: UNT Libraries Government Documents Department
open access

Sampling of power plant stacks for air toxic emissions: Topical report for Phases 1 and 2

Description: Under contract with the US Department of Energy (DE-AC22-92PCO0367), Pittsburgh Energy Technology Center, Radian Corporation has conducted a test program to collect and analyze size-fractionated stack gas particulate samples for selected inorganic hazardous air pollutants (HAPS). Specific goals of the program are (1) the collection of one-gram quantities of size-fractionated stack gas particulate matter for bulk (total) and surface chemical charactization, and (2) the determination of the relationship between particle size, bulk and surface (leachable) composition, and unit load. The information obtained from this program identifies the effects of unit load, particle size, and wet FGD system operation on the relative toxicological effects of exposure to particulate emissions.
Date: February 21, 1995
Partner: UNT Libraries Government Documents Department
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High SO{sub 2} removal efficiency testing. Technical progress report, October--December 1993

Description: This document provides a discussion of the technical progress on DOE/PETC project number DE-AC22-92PC91338, {open_quotes}High Efficiency SQ Removal Testing{close_quotes}, for the time period 1 October through 31 December 1993. The project involves testing at six full-scale utility flue gas desulfurization (FGD) systems to evaluate low capital cost upgrades that may allow these systems to achieve up to 98% SO{sub 2} removal efficiency. The upgrades to be evaluated mostly involve using additives in the FGD systems. The {open_quotes}base{close_quotes} project involved testing at the Tampa Electric Company Big Bend station. All five potential options to the base program have been exercised by DOE, involving testing at the Hoosier Energy Merom Station (Option 1), the Southwestern Electric Power Company Pirkey Station (Option 11), the PSI Energy Gibson Station (Option III), the Duquesne Light Elrama Station (Option IV) and the New York State Electric and Gas Company Kintigh Station (Option V). As of December 1993, testing has been completed for the base project and for Options I and II, has begun but is only partly completed for Options III and IV, and has not yet begun for Option V. The remainder of this document is divided into four sections. Section 2, Project Summary, provides a brief overview of the status of technical efforts on this project. Section 3, Results, summarizes the outcome from these technical efforts during the quarter. Results for each site for which there were significant technical efforts are discussed in separate subsections. In Section 4, Plans for the Next Reporting Period, an overview is provided of the technical efforts that are anticipated for the first quarter of calendar year 1994. Section 5 includes a brief acknowledgment.
Date: January 19, 1994
Creator: Blythe, G.
Partner: UNT Libraries Government Documents Department
open access

High SO{sub 2} removal efficiency testing. Technical progress report, [October 1--December 31, 1992]

Description: Baseline testing at the ``base`` site. Tampa Electric Company`s (TECo`s) Big Bend Station, commenced on September 28 and was completed on October 2. Initial results from this testing were presented in the previous Technical Progress Report, but a more complete discussion is provided in this report. Parametric testing was conducted at the Big Bend site during this quarter to evaluate the effects of dibasic acid (DBA) addition on system SO{sub 2} removal performance. The parametric tests were conducted from November 2 through 19. A DBA consumption rate test was also conducted, after the parametric tests were completed. The DBA consumption test was conducted from November 21 through 25. Options I and II to the base program were exercised by DOE/PETC at the end of the previous quarter. These options involve testing at Hoosier Energy Rural Electric Cooperative Inc.`s Merom Station and Southwestern Electric Power Company`s Pirkey Station, respectively. Testing was conducted at Merom Station during November. Previously, Radian Corporation was the test contractor for EPRI-funded performance additive testing at this site. This EPRI-funded testing involved the equivalent of baseline testing, parametric testing with both DBA and sodium formate performance additives, and an additive consumption test with the DBA additive. The results of the prior testing will be available to support the objectives of this DOE project Consequently, the only testing required at the Merom site was to conduct consumption tests with the sodium formate additive. After a brief baseline repeat test, two sodium formate consumption tests were conducted during the time period from November 11 through 23. Results from the consumption tests are presented and discussed in this report.
Date: January 20, 1993
Creator: Blythe, G.
Partner: UNT Libraries Government Documents Department
open access

Field study of disposed wastes from advanced coal processes. Quarterly technical progress report, October--December 1993

Description: The Department of Energy/Morgantown Energy Technology Center (DOE/METC) has initiated research on the disposal of solid wastes from advanced coal processes. The objective of this research is to develop information to be used by private industry and government agencies for planning waste disposal practices associated with advanced coal processes. To accomplish this objective, DOE has contracted Radian Corporation and the North Dakota Energy and Environmental Research Center (EERC) to design, construct and monitor a limited number of field disposal tests with advanced coal process wastes. These field tests will be monitored over a three year period with the emphasis on collecting data on the field disposal of these wastes.
Date: December 31, 1993
Partner: UNT Libraries Government Documents Department
open access

Field study of disposed wastes from advanced coal processes. Quarterly technical progress report, July--September 1992

Description: The Department of Energy/Morgantown Energy Technology Center (DOE/METC) has initiated research on the disposal of solid wastes from advanced coal processes. The objective of this research is to develop information to be used by private industry and government agencies for planning waste disposal practices associated with advanced coal processes. To accomplish this objective, DOE has contracted Radian Corporation and the North Dakota Energy & Environmental Research Center (EERC) to design, construct, and monitor a limited number of field disposal tests with advanced coal process wastes. These field tests will be monitored over a three year period with the emphasis on collecting data on the field disposal of these wastes. There has been considerable research on the characteristics and laboratory leaching behavior of coal wastes -- a lesser amount on wastes from advanced coal processes. However, very little information exists on the field disposal behavior of these wastes. Information on field disposal behavior is needed (a) as input to predictive models being developed, (b) as input to the development of rule of thumb design guidelines for the disposal of these wastes, and (c) as evidence of the behavior of these wastes in the natural environment.
Date: December 31, 1992
Partner: UNT Libraries Government Documents Department
open access

Field study of disposed solid wastes from advanced coal processes. Annual technical progress report, October 1991--September 1992

Description: Radian Corporation and the North Dakota Energy and Environmental Research Center (EERC) are funded to develop information to be used by private industry and government agencies for managing solid wastes produced by advanced coal combustion processes. This information will be developed by conducting several field studies on disposed wastes from these processes. Data will be collected to characterize these wastes and their interactions with the environments in which they are disposed. Three sites were selected for the field studies: Colorado Ute`s fluidized bed combustion (FBC) unit in Nucla, Colorado; Ohio Edison`s limestone injection multistage burner (LIMB) retrofit in Lorain, Ohio; and Freeman United`s mine site in central Illinois with wastes supplied by the nearby Midwest Grain FBC unit. During the past year, field monitoring and sampling of the four landfill test cases constructed in 1989 and 1991 has continued. Option 1 of the contract was approved last year to add financing for the fifth test case at the Freeman United site. The construction of the Test Case 5 cells is scheduled to begin in November, 1992. Work during this past year has focused on obtaining data on the physical and chemical properties of the landfilled wastes, and on developing a conceptual framework for interpreting this information. Results to date indicate that hydration reactions within the landfilled wastes have had a major impact on the physical and chemical properties of the materials but these reactions largely ceased after the first year, and physical properties have changed little since then. Conditions in Colorado remained dry and no porewater samples were collected. In Ohio, hydration reactions and increases in the moisture content of the waste tied up much of the water initially infiltrating the test cells.
Date: December 31, 1992
Partner: UNT Libraries Government Documents Department
open access

Field study of disposed wastes from advanced coal processes. Quarterly technical progress report, April--June 1994

Description: The Department of Energy/Morgantown Energy Technology Center (DOE/METC) has initiated research on the disposal of solid wastes from advanced coal processes. The objective of this research is to develop information to be used by private industry and government agencies for planning waste disposal practices associated with advanced coal processes. To accomplish this objective, DOE has contracted Radian Corporation and the North Dakota Energy & Environmental Research Center (EERC) to design, construct, and monitor a limited number of field disposal tests with advanced coal process wastes. These field tests will be monitored over a three year period with the emphasis on collecting data on the field disposal of these wastes. The specific objectives for the reporting period of April, 1994 to June, 1994 were as follows: collect and analyze third annual samples from Illinois Cell 1; collect and analyze first annual samples from Illinois Cells 2 and 3; complete a draft of the Design Manual; present project results at the AWMA conference; finalize the Colorado Site report; and prepare for sampling at Ohio and Colorado sites.
Date: August 1, 1994
Partner: UNT Libraries Government Documents Department
open access

Field study of disposed wastes from advanced coal processes. Quarterly technical progress report, April--June 1992

Description: The Department of Energy/Morgantown Energy Technology Center (DOE/METC) has initiated research on the disposal of solid wastes from advanced coal processes. The objective of this research is to develop information to be used by private industry and government agencies for planning waste disposal practices associated with advanced coal processes. To accomplish this objective, DOE has contracted Radian Corporation and the North Dakota Energy & Environmental Research Center (EERC) to design, construct, and monitor a limited number of field disposal tests with advanced coal process wastes. These field tests will be monitored over a three year period with the emphasis on collecting data on the field disposal of these wastes. There has been considerable research on the characteristics and laboratory leaching behavior of coal wastes -- a lesser amount on wastes from advanced coal processes. However, very little information exists on the field disposal behavior of these wastes. Information on field disposal behavior is needed (a) as input to predictive models being developed, (b) as input to the development of rule of thumb design guidelines for the disposal of these wastes, and (c) as evidence of the behavior of these wastes in the natural environment.
Date: December 31, 1992
Partner: UNT Libraries Government Documents Department
open access

Field study of disposed wastes from advanced coal processes. Quarterly technical progress report, January--March 1993

Description: The Department of Energy/Morgantown Energy Technology Center (DOE/METC) has initiated research on the disposal of solid wastes from advanced coal processes. The objective of this research is to develop information to be used by private industry and government agencies for planning waste disposal practices associated with advanced coal processes. To accomplish this objective, DOE has contracted Radian Corporation and the North Dakota Energy & Environmental Research Center (EERC) to design, construct, and monitor a limited number of field disposal tests with advanced coal process wastes. These field tests will be monitored over a three year period with the emphasis on collecting data on the field disposal of these wastes. This report describes leach tests and groundwater monitoring.
Date: September 1, 1993
Partner: UNT Libraries Government Documents Department
open access

High SO{sub 2} removal efficiency testing. Technical progress report, [January 1--March 31, 1993]

Description: This document provides a discussion of the technical progress on DOE-PETC Project Number AC22-92PC91338, ``High Efficiency SO{sub 2} Removal Testing,`` for the time period from January 1 through March 31, 1993. The project involves testing at full-scale utility flue gas desulfurization (FGD) systems to evaluate low capital cost upgrades that may allow these systems to achieve up to 98% SO{sub 2} removal efficiency. The options to be evaluated primarily involve the addition of organic acid buffers to the FGD systems. The ``base`` project involves testing at one site, Tampa Electric Company`s Big Bend Station. Up to five optional sites may be added to the program at the discretion of DOE-PETC. By March 31, 1993, four of those five options had been exercised. The options include testing at Hoosier Energy`s Merom Station (Option I), Southwestern Electric Power Company`s (SWEPCo) Pirkey Station (Option II), PSI Energy`s Gibson Station (Option III), and Duquesne Light`s Elrama Station (Option IV). The remainder of this document is divided into three sections. Section 2, Project Summary, provides a brief overview of the technical efforts on this project during the quarter. Section 3, Results, summarizes the outcome of those technical efforts. Results for the Base Program and for Options I and II are discussed in separate subsections. There are no technical results yet for Options III and IV, which were just exercised by DOE-PETC this quarter.
Date: April 22, 1993
Creator: Blythe, G.
Partner: UNT Libraries Government Documents Department
open access

Field study of disposed wastes from advanced coal processes. Quarterly technical progress report, November 1991--January 1992

Description: The objective of this research is to develop information to be used by private industry and government agencies for planning waste disposal practices associated with advanced coal processes. To accomplish this objective, DOE has contracted Radian Corporation and the North Dakota Energy & Environmental Research Center (EERC) to design, construct, and monitor a limited number of field disposal tests with advanced coal process wastes. These field tests will be monitored over a three year period with the emphasis on collecting data on the field disposal of these wastes. Accomplishments for this past quarter are as follows: The 9th quarterly measurements at the Colorado site took place in December, 1991. Permeability and neutron absorption moisture content measurements were made and on site data was collected from the data logger; The 9th quarterly sampling at the Ohio site took place in November 1991. Permeability and moisture content measurements were made, and water samples were collected from the wells and lysimeters; The second quarterly core and water samples from the first Illinois test case were collected in mid November, and field data were collected from the data logger; Chemical analysis of all core and water samples continued; all chemical analyses except for some tests on Illinois second quarter cores are now complete.
Date: August 1, 1992
Partner: UNT Libraries Government Documents Department
open access

High SO{sub 2} removal efficiency testing. Technical progress report

Description: The project involves testing at six full-scale utility flue gas desulfurization (FGD) systems, to evaluate low capital cost upgrades that may allow these systems to achieve up to 98% SO{sub 2} removal efficiency. The upgrades to be evaluated mostly involve using additives in the FGD systems. On the base program, testing was completed at the Tampa Electric Big Bend Station in November 1992. The upgrade option tested was DBA additive. For Option 1, at the Hoosier Energy Merom Station, three upgrade options have been tested: DBA additive, sodium formate additive, and high pH set point operation. Option 2 has involved testing at the Southwestern Electric Power Company Pirkey Station. Both sodium formate and DBA additives were tested as potential upgrade options at Pirkey. On Option 3, for testing at the PSI Energy Gibson Station, a DBA additive performance and consumption test was conducted in late February through mid-March 1994. Preliminary results from these tests are discussed in Section 3 of this progress report. Option 4 is for testing at the Duquesne Light Elrama Station. The FGD system employs magnesium-enhanced lime reagent and venturi absorber modules. An EPRI-funded model evaluation of potential upgrade options for this FGD system, along with a preliminary economic evaluation, determined that the most attractive upgrade options for this site were to increase thiosulfate ion concentrations in the FGD system liquor to lower oxidation percentages and increase liquid-phase sulfite alkalinity, and to increase the venturi absorber pressure drop to improve gas/liquid contacting. Parametric testing of these upgrade options was conducted in late March 1994. Preliminary results from these tests are also discussed in Section 3 of this progress report.
Date: April 28, 1994
Creator: Blythe, G.
Partner: UNT Libraries Government Documents Department
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