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Preliminary Results of Altitude-Wind-Tunnel Investigation of X24C-4B Turbojet Engine. 4 - Performance of Modified Compressor, Part 4, Performance of Modified Compressor

Description: The performance of the 11-stage axial-flow compressor, modified to improve the compressor-outlet velocity, in a revised X24C-4B turbojet engine is presented and compared with the performance of the compressor in the original engine. Performance data were obtained from an investigation of the revised engine in the MACA Cleveland altitude wind tunnel. Compressor performance data were obtained for engine operation with four exhaust nozzles of different outlet area at simulated altitudes from 15,OO… more
Date: December 22, 1947
Creator: Thorman, H. Carl & Dupree, David T.
Partner: UNT Libraries Government Documents Department
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Tests of the AN/SPS-1 Radar Antenna in the Langley Full-Scale Tunnel

Description: Tests have been conducted to determine the drive-motor torque and the static force and moment characteristics of the AN/SPS-1 radar antenna. Shifting the longitudinal position of the antenna had very little effect on the drive-motor torque, which reached a maximum value expressed in terms of dynamic pressure (T/q)(sub max) of 1.15 at an azimuth angle of 245. The maximum observed values of rolling, pitching, and yawing moments in terms of dynamic pressure are -29.0, 66.6, and 13.4, respectively.
Date: December 22, 1947
Creator: May, Ralph W., Jr.
Partner: UNT Libraries Government Documents Department
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