Preliminary Results of Altitude-Wind-Tunnel Investigation of X24C-4B Turbojet Engine. 4 - Performance of Modified Compressor, Part 4, Performance of Modified Compressor
Description:
The performance of the 11-stage axial-flow compressor, modified to improve the compressor-outlet velocity, in a revised X24C-4B turbojet engine is presented and compared with the performance of the compressor in the original engine. Performance data were obtained from an investigation of the revised engine in the MACA Cleveland altitude wind tunnel. Compressor performance data were obtained for engine operation with four exhaust nozzles of different outlet area at simulated altitudes from 15,OO…
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Date:
December 22, 1947
Creator:
Thorman, H. Carl & Dupree, David T.
Item Type:
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Partner:
UNT Libraries Government Documents Department