Prediction of Kizildere reservoir behavior under exploitation

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Kizildere geothermal reservoir is under exploitation since 1984. During the four years of operation, electricity production showed a decline from the initially designed power output of 20.4 MW{sub e}. The scaling in wells necessitates periodic mechanical cleaning. However decline in well flow rates even after cleaning, indicate either decrease in productivity index due to scaling in fractures or due to rapid decline in reservoir pressure due to insufficient recharge and strong interference between wells. In this paper the results of a lumped parameter model prepared for Kizildere will be presented with the analysis of natural state of the field.

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317-321

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Okandan, Ender January 1, 1988.

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Description

Kizildere geothermal reservoir is under exploitation since 1984. During the four years of operation, electricity production showed a decline from the initially designed power output of 20.4 MW{sub e}. The scaling in wells necessitates periodic mechanical cleaning. However decline in well flow rates even after cleaning, indicate either decrease in productivity index due to scaling in fractures or due to rapid decline in reservoir pressure due to insufficient recharge and strong interference between wells. In this paper the results of a lumped parameter model prepared for Kizildere will be presented with the analysis of natural state of the field.

Physical Description

317-321

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  • Proceedings, thirteenth workshop on geothermal reservoir engineering, Stanford University, Stanford, CA, January 19-21, 1988

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  • Report No.: SGP-TR-113-45
  • Grant Number: AS07-84ID12529
  • Office of Scientific & Technical Information Report Number: 887300
  • Archival Resource Key: ark:/67531/metadc886325

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  • January 1, 1988

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  • Sept. 21, 2016, 2:29 a.m.

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  • Dec. 6, 2016, 4:19 p.m.

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Okandan, Ender. Prediction of Kizildere reservoir behavior under exploitation, article, January 1, 1988; United States. (digital.library.unt.edu/ark:/67531/metadc886325/: accessed August 24, 2017), University of North Texas Libraries, Digital Library, digital.library.unt.edu; crediting UNT Libraries Government Documents Department.