IMPROVED MISCIBLE NITROGEN FLOOD PERFORMANCE UTILIZING ADVANCED RESERVOIR CHARACTERIZATION AND HORIZONTAL LATERALS IN A CLASS I RESERVOIR--EAST BINGER (MARCHAND) UNIT

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Description

Implementation of the work program of Budget Period 2 of the East Binger Unit (''EBU'') DOE Project continues. The drilling of new horizontal well EBU 63-2H, scheduled for this reporting period, was delayed due to a lack of rig availability. This well was spud near the end of the reporting period. EBU 59-1 was converted to injection service, and injection capacity at the plant was increased from 19 MMscf/d to 22 MMscf/d. Although other factors have temporarily limited the field's ability to fully utilize the increased capacity, injection in the pilot area has been increased over 2 MMscf/d since the ... continued below

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14 pages

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Sinner, Joe August 19, 2003.

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Description

Implementation of the work program of Budget Period 2 of the East Binger Unit (''EBU'') DOE Project continues. The drilling of new horizontal well EBU 63-2H, scheduled for this reporting period, was delayed due to a lack of rig availability. This well was spud near the end of the reporting period. EBU 59-1 was converted to injection service, and injection capacity at the plant was increased from 19 MMscf/d to 22 MMscf/d. Although other factors have temporarily limited the field's ability to fully utilize the increased capacity, injection in the pilot area has been increased over 2 MMscf/d since the start of the project. Nitrogen recycle within the pilot area has been reduced with the projects implemented to date. Prior to pilot development, nitrogen production was 56% of nitrogen injected. Currently, nitrogen production is only 26% of injection. Pilot area oil production has increased 90 bpd or 30%, with 160 bpd from new wells offset by a loss of 70 bpd from wells converted to injection.

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14 pages

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OSTI as DE00824381

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  • Other Information: PBD: 19 Aug 2003

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  • Report No.: NONE
  • Grant Number: FC26-00BC15121
  • DOI: 10.2172/824381 | External Link
  • Office of Scientific & Technical Information Report Number: 824381
  • Archival Resource Key: ark:/67531/metadc783435

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Office of Scientific & Technical Information Technical Reports

Reports, articles and other documents harvested from the Office of Scientific and Technical Information.

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  • August 19, 2003

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  • Dec. 3, 2015, 9:30 a.m.

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  • Jan. 3, 2017, 2:25 p.m.

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Sinner, Joe. IMPROVED MISCIBLE NITROGEN FLOOD PERFORMANCE UTILIZING ADVANCED RESERVOIR CHARACTERIZATION AND HORIZONTAL LATERALS IN A CLASS I RESERVOIR--EAST BINGER (MARCHAND) UNIT, report, August 19, 2003; United States. (digital.library.unt.edu/ark:/67531/metadc783435/: accessed January 17, 2018), University of North Texas Libraries, Digital Library, digital.library.unt.edu; crediting UNT Libraries Government Documents Department.