Post waterflood CO{sub 2} miscible flood in light oil fluvial - dominated deltaic reservoirs. Fourth quarterly progress report, July 1, 1995--September 30, 1995

PDF Version Also Available for Download.

Description

Production from the Marg Area 1 at Port Neches is averaging 222 BOPD for this quarter. The production drop is due in part to mechanical problems and to poor sweep efficiency caused by water blockage that prevented the CO{sub 2} from contacting new residual oil deeper in the reservoir. Alternating water and gas injection assisted to some extent in maintaining oil production and improved the reservoir yield by reducing the gas production. A workover was performed on well Kuhn No. 38 to correct failed gravel pack setting. Production from the well was restored to 60 BOPD. Plugging of the injection ... continued below

Physical Description

12 p.

Creation Information

Creator: Unknown. November 10, 1995.

Context

This report is part of the collection entitled: Office of Scientific & Technical Information Technical Reports and was provided by UNT Libraries Government Documents Department to Digital Library, a digital repository hosted by the UNT Libraries. More information about this report can be viewed below.

Who

People and organizations associated with either the creation of this report or its content.

Creator

  • We've been unable to identify the creator(s) of this report.

Sponsor

Publisher

Provided By

UNT Libraries Government Documents Department

Serving as both a federal and a state depository library, the UNT Libraries Government Documents Department maintains millions of items in a variety of formats. The department is a member of the FDLP Content Partnerships Program and an Affiliated Archive of the National Archives.

Contact Us

What

Descriptive information to help identify this report. Follow the links below to find similar items on the Digital Library.

Description

Production from the Marg Area 1 at Port Neches is averaging 222 BOPD for this quarter. The production drop is due in part to mechanical problems and to poor sweep efficiency caused by water blockage that prevented the CO{sub 2} from contacting new residual oil deeper in the reservoir. Alternating water and gas injection assisted to some extent in maintaining oil production and improved the reservoir yield by reducing the gas production. A workover was performed on well Kuhn No. 38 to correct failed gravel pack setting. Production from the well was restored to 60 BOPD. Plugging of the injection wells continue to be a problem, reducing the injection rate in critical areas of the reservoir, near well Kuhn No. 15R. Texaco drilled the well Polk B No. 39 to The Marg Area 3 reservoir to gain structural position based on the 3D seismic, and found the sand present as anticipated. However, the sand did not have any hydrocarbon accumulation. For this reason, Texaco will abandon testing the idea of utilizing CO{sub 2} to accelerate the primary production rate and reduce water production and primary production cycle time, in the reservoir.

Physical Description

12 p.

Notes

OSTI as DE96004699

Source

  • Other Information: PBD: 10 Nov 1995

Language

Item Type

Identifier

Unique identifying numbers for this report in the Digital Library or other systems.

  • Other: DE96004699
  • Report No.: DOE/BC/14960--12
  • Grant Number: FC22-93BC14960
  • DOI: 10.2172/181499 | External Link
  • Office of Scientific & Technical Information Report Number: 181499
  • Archival Resource Key: ark:/67531/metadc665133

Collections

This report is part of the following collection of related materials.

Office of Scientific & Technical Information Technical Reports

Reports, articles and other documents harvested from the Office of Scientific and Technical Information.

Office of Scientific and Technical Information (OSTI) is the Department of Energy (DOE) office that collects, preserves, and disseminates DOE-sponsored research and development (R&D) results that are the outcomes of R&D projects or other funded activities at DOE labs and facilities nationwide and grantees at universities and other institutions.

What responsibilities do I have when using this report?

When

Dates and time periods associated with this report.

Creation Date

  • November 10, 1995

Added to The UNT Digital Library

  • June 29, 2015, 9:42 p.m.

Description Last Updated

  • Dec. 3, 2015, 6:04 p.m.

Usage Statistics

When was this report last used?

Yesterday: 0
Past 30 days: 0
Total Uses: 2

Interact With This Report

Here are some suggestions for what to do next.

Start Reading

PDF Version Also Available for Download.

Citations, Rights, Re-Use

Post waterflood CO{sub 2} miscible flood in light oil fluvial - dominated deltaic reservoirs. Fourth quarterly progress report, July 1, 1995--September 30, 1995, report, November 10, 1995; United States. (digital.library.unt.edu/ark:/67531/metadc665133/: accessed November 18, 2017), University of North Texas Libraries, Digital Library, digital.library.unt.edu; crediting UNT Libraries Government Documents Department.