Preliminary Performance Data on Westinghouse Electronic Power Regulator Operating on J34-WE-32 Turbojet Engine in Altitude Wind Tunnel

One of 5,157 reports in the series: NACA Research Memorandums available on this site.

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Description

"The behavior of the Westinghouse electronic power regulator operating on a J34-WE-32 turbojet engine was investigated in the NACA Lewis altitude wind tunnel at the request of the Bureau of Aeronautics, Department of the Navy. The object of the program was to determine the, steady-state stability and transient characteristics of the engine under control at various altitudes and ram pressure ratios, without afterburning. Recordings of the response of the following parameters to step changes in power lever position throughout the available operating range of the engine were obtained; ram pressure ratio, compressor-discharge pressure, exhaust-nozzle area, engine speed, turbine-outlet temperature, fuel-valve … continued below

Physical Description

171 p. : ill.

Creation Information

Ketchum, James R.; Blivas, Darnold & Pack, George J. October 27, 1950.

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This report is part of the collection entitled: National Advisory Committee for Aeronautics Collection and was provided by the UNT Libraries Government Documents Department to the UNT Digital Library, a digital repository hosted by the UNT Libraries. It has been viewed 480 times, with 16 in the last month. More information about this report can be viewed below.

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  • Main Title: Preliminary Performance Data on Westinghouse Electronic Power Regulator Operating on J34-WE-32 Turbojet Engine in Altitude Wind Tunnel
  • Series Title: NACA Research Memorandums

Description

"The behavior of the Westinghouse electronic power regulator operating on a J34-WE-32 turbojet engine was investigated in the NACA Lewis altitude wind tunnel at the request of the Bureau of Aeronautics, Department of the Navy. The object of the program was to determine the, steady-state stability and transient characteristics of the engine under control at various altitudes and ram pressure ratios, without afterburning. Recordings of the response of the following parameters to step changes in power lever position throughout the available operating range of the engine were obtained; ram pressure ratio, compressor-discharge pressure, exhaust-nozzle area, engine speed, turbine-outlet temperature, fuel-valve position, jet thrust, air flow, turbine-discharge pressure, fuel flow, throttle position, and boost-pump pressure" (p. 1).

Physical Description

171 p. : ill.

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  • URL: http://hdl.handle.net/2060/20090026535 External Link
  • Report No.: NACA-RM-SE50J11
  • Center for AeroSpace Information Number: 20090026535
  • Archival Resource Key: ark:/67531/metadc65572

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National Advisory Committee for Aeronautics Collection

The National Advisory Committee for Aeronautics (NACA) was a U.S. federal agency founded on March 3, 1915 to undertake, promote, and institutionalize aeronautical research. On October 1, 1958 the agency was dissolved, and its assets and personnel transferred to the newly created National Aeronautics and Space Administration (NASA).

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Creation Date

  • October 27, 1950

Added to The UNT Digital Library

  • Nov. 17, 2011, 5:13 p.m.

Description Last Updated

  • June 18, 2018, 4:15 p.m.

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Ketchum, James R.; Blivas, Darnold & Pack, George J. Preliminary Performance Data on Westinghouse Electronic Power Regulator Operating on J34-WE-32 Turbojet Engine in Altitude Wind Tunnel, report, October 27, 1950; (https://digital.library.unt.edu/ark:/67531/metadc65572/: accessed April 25, 2024), University of North Texas Libraries, UNT Digital Library, https://digital.library.unt.edu; crediting UNT Libraries Government Documents Department.

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