The status of government sponsored projects undertaken to increase gas production from low-permeability gas sands of the western United States during August 1978 is summarized. Background information is given in the September 1977 Status Report, NVO/0655-100. One of the largest massive Hydraulic Fracture (MHF) treatment to date was performed on Gas Producing Enterprises Well No. CIGE 2-29. C.H. Atkinson, Western Gas Sands Project (WGSP) Manager and D.C. Bleakly, CER Corporation were observers. Oriented coring operations on the Mitchell Energy well, Muse-Duke No. 1 were observed by Atkinson and Bleakly near Mexia, Texas. The Fourth Annual Department of Energy Symposium on Enhanced Oil and Gas Recovery and Improved Drilling Methods was held on August 29-31, 1978 in Tulsa, Oklahoma. The USGS continued geological and geophysical studies in the four primary study areas. Low-level oblique photography of Tertiary and Cretaceous rocks exposed in the Rock Springs Uplift area was completed, and core from the J.C. Paine well in Montana was sampled for petrograhic analysis. Bartlesville Energy Technology Center continued work on the improved pressure coring system and anticipates completion of the project by September 30, 1978. Preliminary work began on the Parametric Analysis of MHF Test Data, an Engineering Study of Western Gas Sands, by Intercomp. The National Laboratories, funded by DOE are continuing their work in the area of research and development. The emphasis is on instrumentation systems, rock mechanics, mathematical modeling, and data analysis. The Mitchell Energy well, Muse Duke No. 1, has reached total depth and was logged on August 31, 1978. The DOE well test facility was moved from the RB-MHF 3 well in Colorado to Vernal, Utah for trailer modifications and checkout.